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Topic - Ford Escorts
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Petter Handyman Oil Engine No. 23345
Mechanical Repairs
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The main mechanical issue was
the badly bent crankshaft. The bend was too severe to leave
therefore the only option was to have the crankshaft straightened.
This was considered a risky procedure as there was no way
of knowing whether the shaft would snap or crack under the
strain of being straightened. As we were not confident enough
to attempt repair ourselves we utilised a local engineering
company to undertake the repair. Having discussed the repair
procedure with the engineering shop, the crankshaft was set
up on a large surface plate to assess the 'damage' and establish
the correct point at which to apply heat and pressure. The
repair went ahead and a few days later we got a call to collect
the crankshaft. When we arrived the crankshaft was already
set up on a lathe to demonstrate it was running true. We are
quite confident the crankshaft had been successfully repaired,
however it is always worth bearing in mind that heating, cooling
and force can potentially weaken metal components therefore
we will ensure the crankshaft is regularly inspected for any
defects prior to running the engine.
- The broken air / fuel inlet assembly as shown
in 'Detailed Inspection' was
the other major issue to overcome. Initially we thought that
this damage occured when the engine was dragged out of it's
original place of work. However on closer inspection there appears
to be saw marks on one half of the valve, almost as if a portion
was sawn through and then the rest was literally snapped off.
Hopefully as time goes on we will find out further details of
the engine's original place of work and perhaps why this damage
occured. To repair the valve we considered 'jigging' the assembly
with a tightly fitting mandrel and silver soldering the parts
together. To guarantee an exact alignment would be very difficult
as the assembly was not only snapped but distorted and not parallel.
As the carrier had to be absolutely parallel to allow the slide
to freely move, and also a very close fit to ensure the engine
was controlled correctly we considered the best option was to
have a replacement manufacturerd. A new inlet valve assembly
was made by a fellow enthusiast who reproduced the part to the
original specifications. Using the original valve flange, the
remains of the old slide carrier was cut off the flange and
the flange machined to accept a new slide carrier section which
was machined from a solid piece of brass to the exact dimensions
of an original item. The whole assembly was then soldered together
resulting in an almost invisible repair. Click on the photo
to enlarge.


- As the fuel tank bung was missing....
These pages will be updated periodically as mechanical
repairs are identified and carried out.
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